Wednesday, May 8, 2013

Polysix - Bending Over the Capacitors

Dear Readers, I'm sorry.  Back when I described how I prepared my new keybed for installation into my Korg Polysix, I made it sound fairly straight-forward with no real hiccups.  Sure, at the end, I mentioned something about how a couple of capacitors might have been a little too tall, but this was actually quite a large understatement.  It turns out that those "too tall" capacitors required that I boost up the keybed even further than shown originally, which then prevented the Polysix's control panel from closing.  It was ugly and frustrating and disheartening.  Here's a description of how I fixed the problem.

Here Are the Offending Capacitors That Interfere with the Keybed
As you can see in the picture above, there are two groups of offending capacitors.  Both sets of caps happen to be on KLM-366.  The first group are the six tall Mylar caps (C31-C36) that are part of the "hold" circuits between IC29 and IC25.  The second group of interfering caps include the tall Mylar cap C23 and the stout electrolytic cap C22, both of which are part of the pitch-correction feedback circuit.  At first, I thought that the solution might be to replace all the caps with smaller ones (such as ceramics).  But after a brief exchange with the Polysix Yahoo Group, I considered alternate approaches.  With fresh eyes, it seemed like the best plan was to simply bend over the capacitors so that they weren't as tall.  Easy!

Could I Just Tip the Capacitors to the Side to Make Them Less Tall?
Unfortunately, the caps were mounted very close to the PCB and didn't have enough of their leads above the board to enable me to tip them over.  Since I just replaced an IC on this PCB, though, I have the synth all apart and, therefore, I have full access to the bottom side of KLM-366.  Looking closely, I saw that each cap had a little bit more of its legs sticking out below the PCB.  So, I got out my soldering iron, I applied some heat to the tips of the legs until the solder melted, and then I pushed until I couldn't see the tips of the legs anymore.  See the picture below.

Looking at the Underside of the PCB.  Making the Caps Taller By Pushing on the Tips of their Legs.
Once I did this, the first cap was now taller than it had been because of the extra bit of each leg that I pushed back above the PCB.  Now it was tall enough that I could tip it over with ease.

Bending Over Worked well for the First Cap.  Now for the rest...
After repeating the process for the remaining five capacitors, things are looking pretty good.  Now it's time for the other two caps.

The Six "Hold" Caps Are Done.  Now It's Time for C22 and C23.
The tall Mylar cap on the left side of the picture above was easy to address -- I simply did the same trick of re-heating the solder joint and pushing up the extra bit of each leg.  Then, I bent him over.  The electrolytic cap, though, was too stout (too fat) to push over.  Having a bunch of electrolytic caps on hand, I decided that it would be easier to just replace this guy with one that was skinnier and that had long enough legs to bend over.  So, I de-soldered the old one and soldered in the new one.  I bent it over and, as you can see below, everything is shorter than it was before.

All the Caps are Now Much Shorter Than Before.
With all of the steps complete, I put the keybed back into the synth.  Did it fit?  Well, the part of the keybed that was near the caps fit great.  That problem was solved.  But, with that part of the keybed sitting correctly, it now revealed that another part of the keybed was interfering with something within the case of the Polysix.  A little poking around showed that the long white bar of plastic that I added to my keybed wanted to sit right on top of the rail that holds the whole front side of the KLM-366 and KLM-367 boards.  That's an easy fix that I'll talk about later (just cut that darned plastic bar!).  For now, though, we can be content that this cap-bending job was the key.  It was the key to enabling the keybed to sit properly in the Polysix's case and for the lid to close properly and for the whole thing to be beautiful.  Ah...joy...

Sunday, May 5, 2013

Killing and Reviving my Polysix (Replacing a Dead IC)

So far, I've been pretty successfull with hacking aftertouch, portamento, and detuning into my Korg Polysix .  My next big goal is the addition of velocity sensitivity, which requires me to better understand the VCF control circuitry on KLM-366.  Well, in probing the clock signals for the VCF multiplexing, I killed my Polysix!  This is the story of how I brought her back to the land of the living.

Probing IC12 on KLM-366.  I think that I've found the problem.
How Did I Kill It?  This all started when I was probing around the part of the KLM-366 board that processes the VCF EG signal for each voice.  Specifically, I was exploring the time-division multiplexing of the VCF EG through IC24 and IC23 .  This multiplexing is all kept in sync via clock signals "A", "B", "C", and "INH" that are generated from IC11 and IC12 (schematic below).  In probing IC12, I accidentally shorted one of the pins on IC12 (likely pin 11), which apparently killed it.  As you can see in the pictures above, the "B" signal is clearly bad (it is supposed to be a square wave pulse).


How Do I Fix It?  Replacing IC12 seemed like the only reasonable answer.  The chip itself is really cheap (68 cents).  The hardest part in replacing the IC is disassembling the synth so that I can get good access to the circuit board.  I don't like taking it apart because it gives me too many opportunities to loose screws and to re-connect connectors in the wrong place and stupid stuff like that.  But, in this case, I think that it needs to be done.

Shopping List:  The only part that I really needed was a replacement 14024 chip.  Like usual, I got it from Digikey.  The specific part that I bought was MC14024BCPGOS-ND.  I chose this part because (I think) it is the only through-hole version of the 14024 that they sell.  At 68 cents, I bought 2, just in case I damaged one during my installation.  Also, following the advice from The Old Crow, I decided to install an IC socket at IC12 in order to ease any future replacement of this chip. There are tons of choices for sockets.  Never buy the cheapest ones.  I liked the look of A32869-ND.  Even though it was only 78 cents, it seemed to be one of the higher end models.  Cool.

Removing the Dead IC.  The replacement process starts by removing the dead chip.  Some helpful folks at my workplace suggested that removing an IC is best done by first snipping off each of its legs so that the body of the IC just falls free of the PCB.  Then, as long as you snipped the legs high enough away from the board, there's plenty of leg left to grab with your pliers so that you can apply a little heat and lift each leg out one-by-one.  Pretty easy.

Snip Each Leg of the IC
All Legs Are Snipped, The Body is Loose, and the Legs are Still in the PCB.
Removing Each Leg from the PCB.
Removing the Old Solder:  Even after removing the IC's legs, there was lots of old solder that is plugging the holes in the PCB.  In order to get the new IC socket into all those holes, it's usually best to remove that old solder.  There are a few ways that you can do this -- solder wick and a solder pump being the two most common.  Clearing plugged through-holes is a perfect task for a solder pump.  With a solder pump, you first apply your soldering iron to the hole until the solder melts.  Then, you quickly put the spring-loaded solder pump over the hole and, while the solder is still melted, you hit the release button.  BANG!  The pump pops open and (hopefully) sucks out the liquid solder.  Because I'm new to this, I usually had to try 3-4 times before I got the solder out.  As you can see below, the holes looked fairly clear when I was done.

Using a solder pump to suck out the solder from the holes.
The holes are now fairly clean and ready for the new IC (or socket).
Installing the IC Socket:  At this point, I was able to insert my new IC socket into the holes in the PCB (see below).  It fit pretty nicely.  Now I just needed to solder it in.  Unfortunately, one really needs access to the bottom of the PCB to do this, which means the synth needs to be partly disassembled.  So, I removed the keybed, I removed the rail holding down the PCBs, and I unscrewed all the screws holding down the PCB.  I then removed a few (but not all!) of the multi-pin connectors so that I could tip up the PCB and get access to the bottom (see pic below...the power drill is holding the PCB upright).   Once I was able to access the bottom of the PCB, I was soldered the legs of the IC socket to the PCB.  We're cooking right along now!  Smell the solder!

Inserting the IC Socket.  It fits!
Getting access to the bottom of the PCB.
Soldering the legs of the IC Socket.  Heat the site and THEN apply the solder.
Finishing Up:  Once the socket was soldered in, I layed the PCB back down and I inserted the replacement 14024 IC into the new socket (see pic below).  I then re-attached all the connectors that I had undone, I double checked that I re-connected everything correctly, and I turned on the power.  With the oscilloscope, I checked the "A", "B", and "C" clock signals being generated by the new 14024 (see pic below).  Everything seems to work!

The replacement 14024 IC is nestled into its new home on my KLM-366.
After Replacing IC12, the clock signals all look good.
Oh, The Joy:  With the circuit looking like it's working again, I re-attached the keybed, closed the lid, and fired her up.  Here's my little jam of joy...the playing is crappy, but it's so good to hear her voice again.


Next Step: Tipping over the capacitors so that the keybed fits properly